Boeing 737-5L9, G-MSKA
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Boeing 737-5L9, G-MSKA
Boeing 737-5L9, G-MSKA
AAIB Bulletin No: 6/98 Ref: EW/G98/04/08
Category: 1.1
Aircraft Type and Registration:
Boeing 737-5L9, G-MSKA
No & Type of Engines:
2 CFM56-3B1 turbofan engines
Year of Manufacture:
1990
Date & Time (UTC):
14 April 1998 at 1820 hrs
Location:
Near Birmingham Airport
Type of Flight:
Public Transport (Passenger)
Persons on Board:
Crew - 7 - Passengers - 49
Injuries:
Crew - None - Passengers - None
Nature of Damage:
Nil
Commander's Licence:
Airline Transport Pilot's Licence
Commander's Age:
37 years
Commander's Flying Experience: 6,141 hours (of which 625 were on type)
Last 90 days - 105 hours
Last 28 days - 19 hours
Information Source:
Aircraft Accident Report Form submitted by the pilot
As the aircraft was descending towards Birmingham Airport a single meal was put into the (empty)
No 1 oven in the forward galley; the meal was taken out after one minute, and the oven was
switched off at the controller. After about a minute a smell of burning was apparent and the oven
was opened, but no problems were evident. Approximately 30 to 40 seconds later the smell was
getting worse, so it was again checked and a bright red glow was seen around the back of the rear
internal oven panel. The purser then informed the flight deck that the oven was on fire. A PAN call
was made and an expeditious approach was given by ATC. The cabin staff discharged a BCF fire
extinguisher into the oven but, in spite of this action, the fire appeared to be getting worse. This
information was passed to the flight crew, who upgraded the emergency to a MAYDAY, and
advised ATC that their intention was to stop on the runway and assess the fire before initiating an
evacuation. A second BCF extinguisher was then discharged into the oven.
After the aircraft had stopped the purser checked the oven and was satisfied that the fire was
completely extinguished, he declared that the fire was under control and that it would be safe to
taxy to the stand. The fire brigade escorted the aircraft to the gate as a precaution where a nurse was
in attendance.
The reported fire was caused by an overheated oven element, there had been no smoke or flames,
neither had there been any excessive temperatures outside the oven. The power to the oven went
through four switching devices: a thermostatic controller; an overheat protection trip; a circuit
breaker, and a galley master switch on the flight deck. No attempt was made to pull the circuit
breaker or to operate the galley master switch, indicating that the fire was not recognised as being
an 'electrical' fire. This assumption was not surprising given that a survey of Boeing 737 galley
fires recorded on the CAA MOR database gave over 150 records, the vast majority of which were
caused by the combustion of fat and other food debris left in the oven.
The oven was checked by engineering staff whilst still installed in the aircraft - no defects were
found, so the oven and its controller were examined in the maintenance workshops; again no defect
was found, however, there was evidence of overheating of the oven elements. The oven is powered
by 3-phase 115 volts AC and is fan assisted, there are three heating elements in the oven powered
separately by each phase through a common control relay. Both the oven and the controller were
sent to an overhaul agency who confirmed that one element had been subject to overheating. The
controller did not have any relevant defects.
It is considered that the problem was caused by a control failure; selecting OFF should switch off
the fan and de-energise the heating element control relay. The evidence suggests that one contact of
the relay failed to open when the oven was selected OFF, resulting in the power continuing to one
element. Without the fan to transfer the heat, and the normal thermostatic temperature control being
bypassed by the failure, the element continued to heat until it glowed red. It is probable that
vibration during the landing released the relay contact and allowed the element to cool. The oven
has an overheat protection trip which did not operate (it will not reset itself) and has subsequently
been tested and found serviceable. The conclusion is that it did not get hot enough to operate.
Flight deck and galley procedures are being reviewed as a result of the non-use of the circuit
breaker or the galley master switch.